Picked up my 2014 SE from the dealer today. They had it for 4 days. They had contacted Ford's Hotline and followed their instructions for testing. There were no outstanding TSBS for my build date (3/14). A number of looms and inline connectors were inspected, coolant pump was checked. Apparently the car was connected to an electrical system monitor because they list a .010 amp drain and that 2 to 3 times an hour it recorded a .300 amp drain lasting 10 to 14 seconds which Ford engineering said was the BCM waking up momentarily - a normal operation. Apparently the car was monitored over an extended period of time because the tech mentions overnight current drain results. So, at this point they were not able to find any problem other than the dead battery it came in with :-(. Now it's off to the body shop to get the front end ding repaired.